2016 Ford F-150

  • 2016 Ford F-150

    Ford F-150
    Mileage
    80,759
    Service Date
    9/3/2021
    Services Performed
    • General Inspection – Recommendations – Recommend replacing serpentine belt. Inspection findings – Power Steering Fluid – NA Belts: engine, accessory, serpentine, V-drive – serpentine belt has signs of aging recommend to replace.
    • Removed and replaced oil filter, drain the oil and refilled with 7.7 quarts of 5w 20 full synthetic oil with added BG MOA. Added oil change sticker for 5000 miles at and reset maintenance light.
    • Verified customer concern of vehicle running rough at idle. Performed vehicle pre scan, found no current ECU codes stored at time of testing. Viewed live data and verified bank 2 O2 sensors are reading lean. Inspected for possible vacuum leaks using throttle body cleaner while monitoring O2 sensor data and found no fluctuation in idle or O2 sensor, verifying no external vacuum leaks present at time of testing. Removed air cleaner and verified air filter is clean. Removed air cleaner duct and found throttle body build up, see picture for details. Performed throttle body clean and verified idle quality has improved, recommend performing air induction service. See added line for Air induction service. Re road tested vehicle and monitored live data, during road test found vehicle had slight stumble at stop light, performed relative compression test and verified no abnormal compression issues noted at time of testing, during testing found engines idle dropped to 300 RPM and SEL lit, Scanned code and found P0022-00 -"A" Camshaft position timing _ over-retarded (Bank 2) – Pending DTC, P0315-00 – Crankshaft position variation not learned – Current DTC – Warning lamp on. Attempted to ;perform crank variation relearn, and was un able to due to the current state of the solenoid fault, see lamp scope wave form confirming interm sticking VCT solenoid. Recommending replacing both Bank 2 VCT intake and exhaust VCT's with necessary gaskets to reseal Bank 2 Valve cover.
    • Performed BG air induction service.
    • Replace bank 2 VCT solenoids, found sludge buildup on both solenoids and valve cover, cleaned, installed new VTC solenoid and performed oil change service (See LOF service line). Cleared codes and monitored live data, found slight inconsistencies with exhaust Bank 1 and Bank 2 VCT solenoid readings, performed misfire monitor neutral profile correction due to misfires on cylinder 1 and 6. Monitor live data and verified slight stumble intermittently now currently on cylinder number 3 which is bank 1. Viewed live data and verified a 10 degree difference between Bank 1 VCT and Bank 2 VCT exhaust solenoid, recommending replacing Bank 1 intake and exhaust VCT's in order to prevent customer return for rough idle. Final Tech Notes : No code returned, can feel slight stumble at idle when vehicle is at operating temperature, recommend replacing Bank 1 VCT solenoid to help customer return for rough idle at times.
    • shipping
    • Contacted extended warranty company and they authorized Bank 1 VCT's replacement, replaced passenger side Bank 1 VCT's. Performed misfire reset, road tested while monitoring live data, verified stumble at idle is no longer present after road test, and verified VCT data are with in spec's. Performed post scan to verify repairs.
     
    Chuck F. gave our service a 5 star review on 9/4/2021

Address

CT's Automotive
163 Goldmine Drive Unit B
Pagosa Springs, CO81147
(970) 264-1630

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